I have assembled and configured Bittle according to the documentation. Almost everything works fine, using the IRRemote I can make it trot, crawl, and stretch etc. no problem. However, pressing the walk button results in a short beep and Bittle no longer responding to anything. The same happens when giving a walk command, like kwkF. Does anyone have any idea what causes this issue and how to solve this? Thanks in advance!
That's a great news! Congratulations!
What‘s the size of your compiled file? Are you using the latest OpenCat code from GitHub? A screenshot and video will be more helpful.