Hi,
I'm facing similar issue.
I've loaded Writeinstinct.ino and answer "Y" to every question. Everything was successful but when I'm typing "c" Nybble is only beeping shortly, the serial monitor display the joints values but nothing happen on the Servos. They don't move to calibration mode. I've tried to set some offset but nothing move.
I've checked the servos cables and they are correct. I did several try and servos moved after the Instinct update step.
I didn't receive the battery yet but I've plugged an external power supply with 10Volts (I've tried different voltage from 7.4 to 12Volts)
I've tried to load Nybble.ino, initialization seems to be ok but calibration mode has same behavior as before, servos don't move. And I've also get an overflow message.
Any idea what's wrong there?
Thanks in advance.
Here an extract from Nybble.ino:
* Starting *
Initializing I2C
Connecting MPU6050...
Testing connections...
MPU successful
Initializing DMP...
1336 -108 49 18
Enabling DMP...
Enabling interrupt detection
DMP ready!
* Assigning 0 skill addresses...
Finished!
FIFO overflow! Using last reading!
FIFO overflow! Using last reading!
c
0, 1, 2, 3, 4, 5, 6, 7, 8, 9, 10, 11, 12, 13, 14, 15,
0 0 0 0 0 0 0 0 0 0 0 0 0 0 0 0
c0 0