Hello everybody I received my bittle few days ago. Was playing around a bit and removed the head. After reconnecting the servo the head don't move anymore. I connected it to the slot in the front left place. Just were it should be according to the manual. I tested the servo in a different place and it worked fine, so I'm sure the servo is not damaged. I can't see any damage on the nyboard either. It's a nyboard v1_0 Any recommendations how to solve this?
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Have you connected the servo to pin 11 and updated the definition list? You also need to re-upload WriteInstinct.ino to update the parameters in the static memory.
The head is moving now, but I can't calibrate it.
My screenshot was for branch 2.0.
The current main branch should look like below:
Could you take a close-up look at the circuit board to see if the 12 and 13 pins are connected by some soldering residues along the path towards the chip? Do other pins, such as 10, 5, and 2 work if you swap them?
Yes, you need to upload WriteInstinct.ino, enter anything to get over the saving code block, then upload OpenCat.ino
In OpenCat.h, you can find the pin definition. The head pin is the first on the list.
Did the servo work on the slot before? You may also connect it to an unused pin and modify the pin definition in OpenCat.h and re-upload the program. It may solve the problem.
Hi, could you plug other working servos to the pin of the head's pin? Is the direction of the servo correct? The black wire is GND and should be close to the board as the other servos.